started my day off with eggs, sausage, toast, and potatoes.
just got carbs open - jets and emulsion tubes are all still looking clear and clean. needle is at the fourth position from the top.
checked voltage at coils and got 11.85 with key on. battery voltage with key on was 12.3.
whats next?
Yes Sausage ,potatoes, eggs!!!
My favorite also.
OK...Now lets fill in the gaps.
See this bike is no different than the same bike with 4 into 1 exhaust.
Not much difference. A non stock exhaust.
BTW the float level on that chart says 22mm- makes sense.
That is .866 thousandths. That has to be finished. Has to get done.
My recommendation.
Intake type???
Exhaust type...Looks like a 4 into 2 system from the photo.
Idle jet #42
Main jet size #110
Slide needle 4th position from the top. EDITmiddle position.
Float levels can cause rich running if they are off. Checked???
Mixture screws Stock says 2 full turns. probably would be 1.5 now.The reason it stumbles from 0-1/4 throttle is because of the exhausts.
It is lean at idle .
I would go up one step on the main and one step on the idle jet.
Stock main jet was #100mm
Stock idle jet is #40mm
I would put in a #110 main jet.
I would put in the #42 idle jet.
I bet it will have good throttle response from 0-1/4 then!