Now possible for road test, not perfect but better each time
More adjustments. Float levels were too rich. High fuel level in all 4.
All float tangs were earlier untouched. I had to bend them rather much upwards to the float valves. I had no flowing VM29 carbs 29 years ago as I recall. -Different fuel nowadays that affect the floats?
Photos after adjustments. Now a little bit low to ensure no flowing carbs at idle.
January 29 Update: pilot
20 17.5, main 120, air screws 1/2 turn out
Today even better! Not that rich fat smelly exhaust fumes after change of pilot jets to 17.5. Larger is definitely not actual in my engine. I have tried some combinations the last months.
My worst problems were:- Too early ignition advance caused fuel squirting carbs.
Solved with spring fix, cut 1/2 turn on each spring
- Floats not adjusted, too high fuel level. Fuel Level Gauge Tool from Z1 Enterprises helped to fix it. I was 100% that floats should be OK since I did not have that much problem 30 years ago with these carbs. Therefore only a quick check that all 4 had same measurements.
I might visit my local tuning company and complain about their setup of the carbs I bought new from them 30 years ago Remaining issue:-Clear tube also showed that carb 4 fuel support is not that good. Visible when letting the fuel flow freely out from the clear tube to remove bubbles. Fuel stopped to come after draining the float bowl (the other 3 flowed freely). I think I heard the result today when engine started to sound lean after a few minutes on clean idle, best so far. This might have tricked me to think lean and too small pilots. I got to check/solve this.
Maybe OK when driving the bike leaning it more to the right, fuel will flow easier into 4Next is to change the plugs to typical heat range. I'll try Denso X24ES-U next time
Other parts as written in SUDCO manual. (verified when I had carbs appart)
Air Jet BS30/97
0.9Jet Needle #5DL31-3
Needle Jet #261 Series
0-8Throttle Valve VM29/15
1.5Needles at the middle notch
Float Height: 23 mm is a starting point. Final adjustment by clear tube routine to see the real thing, fuel level.
Carb boots CB750 OEM much stiffer without curved 2-3 boots as Mikuni. Possible when carb rack adjusted, carb 2 10mm closer carb 3.
836cc NOS RC cast pistons that need wider chambers as I have.
Ported K6 head 34mm inlet (F2 valve), std EX. Stage "street" 30 years ago.
CX-7 cam timed with symmetrical lobe center in focus.
Lightened alternator.
I'll wait for road tests. Taking out the engine again is no longer actual. Next winter after road experiences.