When I received the bike back from the Dyno run they had the jetting at: 105 mains, 50 pilots and YY5 needles 3rd position from the top and open stacks. I did the advance spring mod and ran power direct from the battery to the coils to correct my electrical issues. They shop suggested dropping my jets down a step of two after my electrical was corrected.
I reinstalled my ITG socks and made sure they were positioned near the bell of the stacks so the air intakes were not blocked. I change my mains from 105 to 102s. When i dropped my pilots I found the low end hesitated with the sock filters back on so put the pilots back to 50.
My current jetting is: 102 mains, 50 pilots and YY5 needles 3rd position from the top
I went for a 200KM ride on saturday and what I found is from a stopped position when I wind out the bike it is flauless and pulls hard. If i am cruising at 4,000-4,500 RPM and hit WOT the bike bogs. If I drop a gear when cruising at this RPM and hit WOT it puts me in a higher RPM so the bike accelerates quickly. With this jetting my wife told me I blow a little smoke (rich) at the start when I wind the bike out from a stopped position. I am not sure if it would get any better than my current jetting??
Something I find odd with my clutch is when the bike warm up it does not want to go into 1st gear. Sometimes if I gear up to 3rd I can then drop down to 2nd and 1st. Hopefully some adjustment will correct this but does this seem odd?