Can't believe how fast time flies. I was in such a rush to buy the bike now I'm lagging on actually riding it!
Finally got the stuck bolt off. Ended up grinding it a bit + working at it with a cold chisel.
Started with:
Vice grips and a file + equal parts enthusiasm and inexperience let me with:
Finally broke down and bought a dremel:
Replaced the head with a 17mm I found off of ebay. Thanks Bankerdanny!
As far as the battery goes, man, I should have listened/searched this forum first. I ended up getting another clone of the same battery: XT12N12A-4A-1 Xtreme Battery. But just the thought of having a sealed battery makes me sigh a bit.
Replaced the oil pan gasket.
Emptied the oil and put in 20w-50. I know this is a bit of a contentious topic, but I thought 20w-50 would be best for the time being. I plan on changing the oil soon again at any rate.
Replaced the oil filter. It was black as hell and extremely brittle.
Clamped up the carbs.
Replaced the brass gaskets around the exhaust. I was not planning on this - but I had some from the PO, and I ended up taking off the exhaust in order to work on the oil filter bolt easier.
Bike seems to run idle well so long as there is enough gas in the tank. Starts fine from the electric start. Kickstart is a different story - but I think I just need to get the hang of it.
First off, welcome. Looks like a 550 tank to me, how are you cleaning it?
Could well be a 550 tank. PO said 750 so that's what I was repeating.
Here's a picture of the gas tank before. I tried to clean it with vinegar but was unaware of the flash rusting affect:
Ending up cleaning the rest of it out with evaporust.
A few more things to do:
1) rpm cable was being held on with zip ties - need to get another/or secure it somehow. There is also a weird sound near where the RPM cable connects. I assume I hear that because I don't have the cable connected. I might record the sound it and post it here if it continues once I replace the cable.
2) clutch cable need to be adjusted. Seems to grind when I shift to first - doesn't want to shift back to neutral. Didn't ride the bike much as I wasn't comfortable with the sounds the clutch was making. I think if I adjust it right it will be fine. I was messing with it earlier trying to make the clutch softer/easier to pull and ended up making it worse.
3) I put on a fuel filter - but it was plastic and I was afraid it would melt against the engine. I think i'll get something along the lines of this:
http://www.ebay.com/itm/1-4-6mm-Chrome-Glass-Universal-ATV-DIRT-BIKE-Oil-Cleaner-Inline-Fuel-Filter-New-/181431340941?pt=Motorcycles_Parts_Accessories&fits=Make%3AHonda%7CModel%3ACB500&hash=item2a3e268f8d&vxp=mtr I think I cleaned the tank decently enough but the plastic filter caught quite a few metal/junk filaments.
4) I'm about 5'4" so the bike is a little tall for me. Eventually I might try to replace or shave down the current seat.