what did you change ?
I had leaking valves, AFTER paying someone to redo the seats, grind the valves (there were minute fragments embedded in the seats & valve faces from the "pissed ' n ' broke " year), I bought a set of Newway cutters and did the job properly myself.
Due to the draw thru setup I use, burning mix ignited the methanol mix in the plenum (my BOV works well), & due to the remoteness of the salt lake, I tried to minimize the back firing by leaning it off a bit with the power valve (I didn't know about the valves leaking at the time) and put the "jockey" on board, he made it to 4th gear before it backfired, which I heard clearly from the start line a mile away from him,
I guess pre-ignition caused the power drop he felt, and inverted the piston crowns.
The decision was made to de tune it for next year, "stock" cams with 1mm more lift, and heaps of overlap, which would drop the boost from 15 LB, to 10 LB, & hopefully help cool the ceramic topped pistons (the only pistons available for less than $550 each, bare) are Chinese ,,and, as I discovered while checking valve / piston clearances, with 1mm more lift, I had minus point 5 thou" clearance,,,and 16 bent valves (ever so slightly)
A 2mm head gasket is being made, and I'm about to pressure test the valves using a Perspex gasket, and a dead block,,,3 months to go, and so little play time,,,,
Tiny