Well, I ran some tests. Compression was lower than I thought. 70-60-65-78. Oil didn't seem to bump those numbers substantially, so I checked my valves and made some minor adjustments. Afterwards they were 70-70-70-78. Oil did not do anything afterwards, but I think I may need to ride for a while to burn the oil from the pre-adjustment tests first before it would make a difference.
Checked the fuel level with the clear tube method. I think they were all too high, so I lowered them. I'd had issues with this method before - if the petcock was on when I opened the drain plug on the float bowls, the gas would surge and go way higher, as it seemed to create space for the fuel to go and would then overflow. If it was off, I could get a decent reading of the fuel level, I just had to account for her gas that was in the line. Not a great workaround, but I couldn't get why this would happen so I just dealt with it. Today that wasn't happening except for in carb #1, and I got the fuel level to about a quarter inch below the the top of the bowl with the petcock on 2, 3, and 4.
Carb 1 was different. As soon as I opened the petcock, gas rushed into the tube, and rose way over the line. I cut the petcock off, I closed the drain screw, and checked the bowl level only to find it about a half inch from the top - much lower than the tube indicated, which was quickly climbing over the bowl top by about a half inch.
So I screwed on the bowl and just let it fill with the drain plug closed for about a minute. Turned off the petcock, opened the drain screw and the gas slowly crept into the line.... And kept climbing. Over the top of the bowl. I closed the drain screw, removed the bowl and easily determined the gas was no where near that height, even accounting for the drained off gas.
My float needles are good, and keep the inlet closed, I've tested this. But for whatever reason, the tube draws gasoline out of the bowl and if the petcock is on, causes the bowl to overflow. I eventually capitulated and set the gas height to about where he others are, since the clear tube method wasn't cutting it.
Put her all back together and started her. She ran a little rough, and cracking the throttle cold caused it to bog down, but I might try and do another sync and see what my WOT chop looks like again. I'm thinking I still may need 102s since my 3/4 chop was so lean (picture of plug from cylinder 1 included)
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