Quick update:
It's been seven months since the Big Bang Bike got the engine rebuild, I have not ridden it much since then, to be totally honest, once I finished the Kawasaki H2 I really loved riding that bike [sorry Honda only fans].
But, it's Honda week, and I've ridden this bike twice and also rode the K3 Park Racer.
So the Big Bang Bike has clicked over 500 miles since the rebuild and I've decided that is enough of a break-in period so I have been winding out the gears!
The bike sounds good and pulls great and it's faster in my mind [Butt dyno].
Now that I have 341's on it, I want to do the Hondaman mod - drilling 1/2" holes in the 341 pipes. Have any of you done this?
I do have an intermittent issue and not sure what to do? The other day when I rode it, I blew the main fuse twice. Each time, I'd pop a new fuse in and the bike was fine for a while.
Today, rolled the bike out, started right up, went for a short 35 mile ride and no fuse blew.
Not sure where to go from here? Terry suggested putting a 6mm bolt in place of the fuse? Guess that would work!