Alright I've done the following:
Oil Change (oil/filter)
New Plugs (gapped)
Cam Tension
Adjusted Valves
New OEM Points Assembly (gapped and strobe light timed)
Carbs Cleaned
> Bench Synced
>Clear float tube leveled
>New fuel hoses
>New petcock
New Exhaust Boots
New Intake Boots
New K&N Airfilter
New Battery (AGM)
Alright F3 engine in 750K4 frame. (Carbs are from the early K model)
So to start I hooked up all of the gauges to carb 4. Gauge 1, 3, and 4 were pretty much in sync. 2 was -2 compared to the others, so I marked as is.
Then hooked them all up and fired her up.
3 & 4 was hitting around 9
& 2 was hitting around 7 (which makes sense with the -2 variance)
So 2, 3, 4 seem to be in sync, but 1 was hitting around 15. No matter how much screwing of the Throttle Stop Screw or adjusting of the jet needle it Carb 1 wouldn't get any lower. I've double checked the main and pilot jet and both appear to be clear (I can see light through them). I also switched 1 & 4 gauge assuming maybe my initial baseline calibration was off, but once I switched them 4 started to read around 15 and 1 started to read 9
Here's a video:
At the beginning bike is idling at 900-1,000 and then revved to ~2,500-3,000 (twice)