Well I was right the brakes were definitely in need of work and the rear master cylinder was completely seized, but with the help of a grease gun it broke free, the internals look great so I just cleaned everything up and reassembled, filled, bled, and no problems, checked and adjusted the valves twice just for fun, cut the chain off and removed rear tire to inspect and clean, waiting for new electronic ignition, was so impressed with the electronic ignition I installed on my 76 custom NGW GL1000 that I’m not even going to mess with the stock system......