Long time user on the forum but I mainly search and can usually resolve any problems I have from previous users posts. This forum has been a wealth of knowledge to me. I'm pretty stuck on this one though.
I'm looking for help with an issue on my dads CB550K3. He bought the bike just before Christmas in running condition. He test drove before he bought it and as far as he can remember it was running ok. I didn't test drive it myself when he bought it so I can't confirm this. He didn't do more than a few miles and I don't think he got got above 30-40 mph on it.
So since we had snow and ice and couldn't be riding I said i'd give it a once over as the wiring was in a bad enough way. The negative from the battery was just bolted onto a painted area of the frame near the rear mud guard, bare wires were wrapped around each other with just insulation tape around them etc. The positive from the battery had been "repaired" with a piece of copper pipe, see pic below.
Bike is completely stock (Intake exhaust etc.). No smoke of any sort from the exhaust when running.
So it starts and idles fine and sounds perfect. It drives perfectly up to about half throttle which indicates to me the pilot circuit is not an issue. No hanging idle and when idling it's very smooth. Anything above half throttle and it's like it has very little power or acceleration, I can get it up to about 50-60 mph and it'll move along ok at that but open the throttle and there's just no go. It will almost kind of surge I think, not sure how to describe it and it sounds loud through the airbox kind of?? I thought it may have been a fuel starvation issue.
Bike will rev and sound perfect when standing still, you wouldn't think there was an issue until you drive it.
So what I've done so far is the following:
- Wiring removed and all connectors cleaned and new connectors soldered on where they were missing.
- New positive and negative battery cables made up and fitted correctly, all areas of the frame where the grounds connect were sanded down to bare metal before putting back together.
- New o-rings between the intake manifolds and the head, the old ones were gone hard and somebody had pumped gasket sealant in around them.
- New carb insulators between the carbs and the engine.
- New air filter.
- Valve clearances checked and were fine.
- Carbs disassembled and ultrasonically cleaned, the vents were blocked up alright and they were hard to clear. All passages in the carbs were blown through with air and are clear. All jets were cleaned and inspected and appear fine. The emulsion tubes on the main jet were cleaned and appear fine. Original Keihein jets are in them #42 slow jet and #90 mains. Needles are correct type and are in the correct position per the workshop manual, 3rd position(Middle).
- New o-rings fitted on the idle mixture screws as they were missing.
- IMS are set at 3 turns out, 1.5 is stock but the idle was very rough at this and it's perfect at 3.
- Float levels set using the clear tube method. I checked and triple checked these since I've been having this issue.
- New electronic ignition fitted. Timing is set with a strobe timing light and is correct. Advance mechanism is working as it should checked with the timing light.
- New spark plugs (NGK D8EA). New spark plug boots (NGK 5k ohm) wires cut back 1/2" before fitting new boots.
- Coils checked, the secondary circuit on one coil was reading a bit low, 13.90k ohm should be 15k ohm I believe. So I swapped the coils out from another bike which I know is fine and this made no difference.
- Checked for a vacuum leak with WD40 and couldn't find any.
- Carbs balanced using a Morgan Carbtune.
- I had fitted an inline fuel filter and removed this and there is now one new piece of fuel hose between the tank and the carbs. I've checked the flow out of this and it's fine. The tank vent is also clear.
- Tank itself is clean.
- Compression test done when cold and got between 105 and 115 PSI across all four cylinders. I want to redo this when hot for comparison.
I can't think of anything else at this point that could be causing this issue besides mixture... I'm at the point of tearing my hair out on this one