I checked the compression on 1 and 4, then swapped the plugs, both pump up to 100psi on a long snap on gauge, cleaned the #4 pilot jet, adjusted the pilot screws to 3/4 out, checked the #4 float, the level seemed a bit low, fuel stopped flowing with the float down and when I opened the gas cap it began again. I rebuilt that cap in the house last winter. Hmmm. Air bubble in the right fuel hose? It flows downhill as much as possible, no additional filters.
It's not popping or pulsing out of the 4 pipe now, but the annoying exhaust rattle is full time now lol. I may just remove the 341 baffles, that seems to cure the noise.
I wonder if the gas cap vent is making it run lean since the idle is always high after a ride? I'll pop the guts out of it and swap them or fix it.