We got the carbs apart. I should say, Joe got them apart. Pulled the rod (forget the name) that hooks them all to the bell crank. Pulled the needles, which were all set on the middle notch of five. Lowered them 1 notch each, to get a little more lean in the middle. Raised the main jet 1 size from 125 to to 127.50, to richen the top end. Next is put it together and back to the Dyno. I want to wire in a pigtail to the ignition so its not so hard to plug it into the the Dyno.
My long term goal now is to get the hp up and get it ready for the VJMC National Show at Spring Mill State Park next year in Mitchell IN in June or July. I may have to scab together a better exhaust. I've got a 4-1 Kerker header but no muffler. I know there are muffler places to shop. So it will be fun.
Pictures and more updates soon. Got a snarky oil leak hope to get fixed too. Can't tell if its at the crankcase split, the alternator cover or to bearing stand pucks. All are fixable, the lift really helps.