Andy, the first time I had the head off my K1 (1973?) I replaced the original head gasket with a new aftermaket head gasket. The head was carefully reassembled and properly torqued but when I started the engine, oil POURED out the head gasket. It would have pumped itself dry within 30 minutes. I was crushed. I pulled the engine back out and ended up using the original Honda head gasket with no further serious problems, I still have a little seepage. If I ever take the engine out again I will be torquing the head bolts to the high end of the range or maybe a little beyond. Do a search of the archives.