Thanks guys, it has been fun.
#3 quit firing and started pouring gas from the exhaust pipe drain.
After fiddling with spark plug wires for a few minutes, took off the Carburetors, I must not have tightened the low speed jet, it was just hanging there.
While at it I took apart the low speed circuits and re-cleaned all the ports & holes.
On reassembly I got a little aggressive with the jet and broke it off!
1) Drill and clean, clean, clean.
2) Travel to Iron Horse and order new jet for $5.50
Here today!
All my plugs very black, debating decision to try one of the high performance plugs or to just go one hotter because I just don't run the 750 very hard.
I changed to a 17 tooth front sprocket which has increased the RPM a few hundred at 60mph, but this is not enough to keep the plugs clean.
On reading here I also added a few mm to the height of each float. I believe this will make the idle circuit run leaner. Without doing the clear tubing trick I have seen here it is difficult to know for sure but I think I have each float shut off at about 28mm below the rim of each float bowl. Tried buying a float gauge at Iron horse but they can't provide.