Just came back from the dynorun, there's definately a problem somewhere.....
He adjusted the idle A/F ratio, that is really easy if you can measure exhaust gasses. The numbers were good enough.
Then did a couple of runs.
I only brought a printout from the first run.
The bike is way lean on 105 mains. He tried adjusting it by plugging the hole that connects to the emulsifier tube temporarely. Normally that should richen things up about the same as a 20 nr. mainjet. But it didn't really. I did improve the torque at low RPM a lot.
In the printout the torque is about 16 at 50 km/h. It was about twice that on the second run with the airhole temporarely plugged
No matter what he tried, we couldn"t get rid of the lean running at high rpm though.
There was no point in revving it to redline, as it was getting dangerously lean. Idle to about 1/4 trottle was pretty good though.
So I now suspect the electronic ignition is not working properly somehow. If we advanced or retarded the ignitionplate, nothing would change on the dyno, so that's strange...
The bike also uses a lot of oil, so maybe valveseals are not good either (I didn't install the valves myself) Compression is rather good for such a high milage old bike.
It was really fun though. You lean a lot about your bike if you have a good dyno operator. The way these guys analyse a problem is really fun to watch.