maybe timimg for 2/3 is out of whack somewhere ??
All electronic, non-adjustable. I replaced the CDI box to see no change.
BUT IT'S RUNNING NOW.
I switched the coils around and 1/4 still fired so I knew it wasn't a problem with the coils or wires.
After some cranking it and trying to keep it running on two cylinders, the other two seemed to "pop" on and a puff of black smoke came out of the exhaust. The revs would jump 2 or 3000 and then it'd be back to two cylinders. After a while all four cylinders started firing reliably and it would idle with the choke on. It seemed to rev okay, but there were still occasional backfires and pops.
I'm starting to wonder if there was some water in the gasoline or something that just needed to be worked out of the system.
It's still not reliable or road-ready, but I'm leaps and bounds ahead of where I was this morning.
I'll get some new plugs for it tomorrow (if I have time; I'm buying a car, getting a dog, and getting a desk for my wife, all after 12, so busy day).
My other main concern now is that there's something loose in the fuse box. Every once in a while nothing will happen when I turn the key, but if I wiggle the fuse box then everything pops back on. Yesterday I pulled the fuse box out, cleaned all of the connections, and hit everything with dielectric grease. Maybe I'll just have to fasten it in a working position and hope for the best.