Well, I disassembled the motor today to replace the lower O rings and found another issue on the way. The head gasket had a fair bit of oil on especially between 1 & 2 and 3 & 4 at the front of the engine. I think this means the head and cylinders were not mating up properly. I put in slightly shorter dowels, made sure the head and cylinders would touch without the gasket, reinstalled the gasket and torqued it to 175 inch pounds or about 14.5 foot pounds, right in between what the manual says. We tried a compression tester but that didn't work too well and found I had to use a thread chaser in a couple of spark plug holes to clean the threads. I called my friendly Honda expert and he suggested a leak down test so I asked/begged him to do it since I have no knowledge on this test. This may happen on Wednesday. This is aging me rapidly. Further updates as they occur.
Cheers,
Cliff.