Minor set back with the bike but all is great know. The 915 was running excellent with the exception of needed to be tuned but I was not getting 4th or 5th gear.
I must have done something wrong when I shift tumbler / forks back together. The good news I feel like there is nothing I can't do on these bikes now.
Yanked the engine.
Split the cases and fixed the shifting.
Got everything buttoned back up with out a hitch and it shifts better than any cb I have ever been on, something to be said about taking my time.
I also was able to get close to what I thing is optimal tuning of the RS34's by following Doctor D's guidance, thanks. 132.5 mains, 9DZH03 needles middle clip position, 120 pilots and air screw 1/2 turns out. Synched the carbs and it has more power, seat of the pants, than I could have ever imagined... Only a proper dyno tune will tell the entire story onc it is good and broken in.
On another note I picked up my next project, a 1978 cb750f from member Jaguar, Thanks!
The plan for this bike is to make a nice semi stock daily rider with all my take off bits from this build including the 836 engine and CR29's I have waiting.