TG. I just ran out of time to make a run without the stacks, but at the very end I pulled the foam off the stacks and lost 1 hp. I was most concerned just to clean up carburetion and the result seems good.
There probably is a better path I should have followed working on the dyno. This place is accessable and inexpensive since the owner just worked the computer while I ran the bike then disappeared while I made adjustments. Maybe it'll be worth a re-visit some day.
fastbroshi it weighs 322lbs dry with fairing & bellypan.
EDIT: I'm not sure why an A/F reading is meaningless, it was mostly what I was looking for going to the dyno.
The very first run the top end was perfect but was way rich on the needle. Ultimately every time you make a jetting change to alter one circuit, it has an effect elsewhere. I made sure to make one change at a time and dropping the needle 1 position started to lean out the mainjet. Lowering the needle again further took two sizes larger on the main. The last change I installed 1 size larger airjet instead which cleaned up the needle circuit but shows I may be still slightly lean on the mainjet.
I found the exhaust sniffer helped a great deal even if it may not be completely accurate. But as I mentioned.....I'm all ears.