Ok so I resolved my clutch cable issue. Did a little research and decided to shorten my existing cable. So much easier than I thought it would be and now it’s routed correctly and functions perfectly without hitting the exhaust.
First I cut the old end of the cable off with a dremel. Then pulled the cable out and heated the crimped ferrule a bit with a torch and it slid right off. Cut the sheathing with the dremel 2” and reinstalled the ferrule. That part took some time. You can’t just push back the ferrule since it was crimped so I pushed it on the ends of progressively larger and larger drill bits until it got big enough to slide on. Then re-crimped it with some wire crimpers. Next I cut the cable itself so it would have the same stick out as the old cable did. Which in my case was about 3 1/4”. I made it a little shorter at 3” accidentally but that was no problem. You have plenty of adjustment when on the bike.
Made a new barrel nipple out of some brass I had because I didn’t like the idea of drilling and reusing the old one. I could have bought one from VenhillUSA for about 30¢ but with the holiday shipping times being so delayed I didn’t want to deal with it. I had the brass and have a lathe and drill press so why not. Parts are so small I had to channel my inner Clickspring.
Made a bird caging tool out of some scrap angle steel.
The small drilled hole has to be a hair smaller than the cable so it will clamp on it when in the vise but not too small where it mushes or pinches the cable.
Clamped the cable in there and gave it a couple light whacks with a punch.
Heated up some 63/37 solid core solder on a camp stove I set up on saw horses because I don’t have a solder pot. Used a brake caliper piston from a 2003 R6.
As that was coming up to temp I had the cable end soaking in acetone. Then dipped just the bird cage in flux (not too far because you don’t want solder going up the cable, it needs to stay flexible) and slid down the barrel nipple and dipped the whole thing in flux again, just barely enough to cover the nipple. Again, not going too far as to get flux on the cable on the other side of the barrel nipple.
Dipped the cable into the molten solder just enough to cover the barrel nipple. Actually dipped it a few times like one does to build up wax when making a candle. I wanted to be sure the hole in the barrel nipple was full.
The results are a perfect cable end. Honestly, I’m very pleased with myself, haha.