Finally got the new accelerator pump and there was still no heavy squirt. What did make it squirt was tightening up the linkage spring. As stated before when twisting the throttle, the spring force was too weak to push the rod down which activates the pump. Tightening up the spring now forces the rod to fully actuate the pump driving it all the way to the stop. Works good now.
Not sure how I was able to cure the hanging idle but after having the carbs on and off about ten times this is what I did. Adjusted the valves, tightened the cam chain, adjusted the timing, carb sync, new spark plugs, and replaced the stock 35 pilot jets with 38. Very careful whie tightening up the boots. Idles fine now. I wish I knew what the cure was but I don't.
Thanks for all the help and suggestions....