... an update .....
Well, I pulled the carbs down, and kitted them. There was very little evidence of "slugde" in them. No surprises there, as they were cleaned relatively recently.
I did however find that the filters behind the seats were very dirty (the needle & seat were replaced anyhow, although the kit items didnt have the filter) I didn't even realise they were in there, and last time I had the carbs pulled out i didnt even think to remove the seats. The needles were in the mid position. I was a little surprised at this, as I was expecting them to be richened.
I also cleaned the passages that hondaman mentioned. I did feel some "opposition" to the wire i used to clean them in a couple of the carbs.
While they were apart I spent some time setting the float levels. No. 2 was a couple of mm low (approx 24mm). Could this explain why it was running hotter than the others? The others were ballpark, but i spent quite a bit of time getting them all as close as I could.
Ok, so with the new needles, needle & seat, mains (I went back to 120's), new pilots, a bench synch and a good clean, I got it all back together, fired it, let it idle, and did a plug check after it idled for a few minutes. The two outside plugs were a bit sooty, but the two inside looked ok. I was starting to lean towards ignition again, but took it for a ride anyhow. I found that it ran "ok", but had a big flat spot at around 4000rpm (guessing as i dont trust my tacho), and seemed a little lacklustre. The surging was gone (nice & smooth now), and it ran for half an hour with now additional issues. After the ride I pulled it apart again, as there was an obvious (audible) vacuum leak on no.1, which turned out to be a split manifold. After this was fixed I rode it again, and it seemed a little better, but It was still far from perfect.
Despite my better judgement, I had organised to go for a ride (about an hour away), and when my mate turned up, I shrugged my shoulders and through caution to the wind. Whilst the fluctuations were gone, it still had the flat spot, and was woefull at WOT (not to mention slow, and sluggish uphills). If i nailed it (WOT), it just felt sluggish, and as i wound it back off it seemed to kind of catch up. Also, slowly winding it on yielded slightly better results. From what I have been reading on here recently It seemed like rich behaviour, so I put a set of 105 jets in that I found in some F1 carbs I have. The flatspot still seemed to be there, so I was a little dissapointed, however, when i gassed it past this, it really responded, it actually caught me a little by surprise the first time, as it was a little abrupt. I did a standing start run. and it ran quite well, and wound out 30 to 40 kilometers an hour faster before I backed off, above the top speed it had earlier in the day. I'll do some plug chops to find out whether it may need to go a little richer on the mains, but I'm heading in the right direction now.
Any ideas on what the flat spot / hesitation could be? Could it be that the carbs haven't been properly synched yet? I did notice the needles (Napco) appeared to have a different taper compared the to ones I pulled out.
Cheers.