Well it's back
Yes I was on the dyno today and this is what we found
1 could not use more than 1lb of fuel pressure befor it would start to leak
Out the over flow
A, pulled carb to check needle and seat and o ring around seat had turned to
Dust
With that fixed back on the dyno and AF was still lean
Increased fuel pressure and it came down. Increased to 4.5 lbs and AF is at 12.1
Jetting change to run less pressure
??
Running 240 main
The charging system decided to crap out and had to go to a back up
Batterie
We got air/fuel good at 12.1 all the way to red line
But there is a lean spike just as it comes on to the needle
Past that it's flat line 12.1
I have an oil tank that needs better venting
Had some oil spitting out the breather lines
Pulled the filler cap off and all is good but needs to be addressed
We decided to put boost to it but the waste Gate is not working
Needs to be looked at to see why there is no boost
All in all a good day as we FINALY got the AF figured out
More to come
Jim