So, I got the oval pods from bwaller in record time from Canada. They fit perfectly and look sharp. More filter area than the original pods.
I know there is controversy about pods. I'll say i used them very successfully for many years and 10s of thousands of happy miles. I'd been thinking that maybe the difference is that they work better on larger engines. 750+ vs the 500/550s. But more accurately it might be that they work better on something other than the stock carbs. I've never actually used them on stock CB750 carbs, but on the Mikuni smoothbores VM29. Anyway, I'm not anticipating any trouble as this is virtually the same engine I had, just better slicker parts.
The rear brake wasn't adjusting up. I could run the adj nut all the way up, compress the spring, and the pedal still moved too far. An unexpected issue. Remember back, I had the brake "arced" by Racetech, in CA.
http://www.racetech.com/HTML_FILES/BrakeArcing.htmlThey turned the drum to perfectly round. Then they grind the shoes so they fit in the drum optimally. If you ever checked the stock set up, you'd be surprised how little of the shoes actually touch the drum. I'm expecting this to really improve the rear brake. Well, I'm guessing they had to grind so much of the shoes off to get the whole shoe to touch the drum, that it's thrown the adjustment out. So I figured that we could rotate the arm on the brake plate a spline or two to get it to adjust up. This isn't as simple as sounds, as the cam on the brake plate is not splined all the way around, There is a part of it that has no splines. This makes it more difficult to just take it off, rotate it, and slide it back on. The spline of the arm hits the flat spot of the cam. Not wanting to force it on, we took the arm and ground down two of the splines with a Dremel. This was easier than we thought to do, and the arm slid easily on in a position that allowed a good adjustment. On to the next thing.
Time to offer up the exhaust pipe. Marshall Deep Tone 4-1. We'd done a lot of work on these years ago. The headers are all individual. They would not gang up and fit into the header. So we ground them like crazy to where they would fit. Now we have the problem of fitting them to the head. They use the stock "spigot and finned clamp" arrangement. But where they fit up to the spigot, the wall of the pipe, which should compress on clamping, is so stout and thick that we had to spread the clamps way far apart.
Then the bolts to draw the clamp down won't line up with the threads. When we did get a clamp to draw down, it was so difficult to compress the pipe, it never got tight against the spigot, and the clamp bolt broke. It may have been crossthreaded, but still it wasn't going to work.
One of the most disappointing things so far. After struggling with it for 1.5 hours, it was time to call it quits.
While cleaning gutters, I thought of this. I'll cut some more compression relief slots in the header with the trusty Dremel. Then, rather than use the threads in the clamp, I'll drill them out and use a bolt and nut to draw it down. That ought to work.